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As shown in robotology/icub-tech-support#1364, we had to calibrate the left wrist after a maintenance session. We tested the configuration with the researchers and now the robot calibrates well without hand shaking.

@gsisinna gsisinna requested review from davidetome and pattacini May 12, 2022 12:27
@gsisinna gsisinna self-assigned this May 12, 2022
@pattacini pattacini merged commit 64ef90b into robotology:master May 12, 2022
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2 participants