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@gsisinna gsisinna commented Mar 3, 2022

After receiving a maintenance request for the right thumb of iCubErzelli02 I checked the file in /hardware/mechanicals regarding the coupling matrix for the thumb, and this configuration with the minus sign leads to correct functioning without oscillations.

Probably in the past the sign has been changed according to the winding of the cable on the motor pulley. The robot has been tested and all the joints calibrate normally.

@gsisinna gsisinna requested a review from pattacini March 3, 2022 15:33
@gsisinna gsisinna self-assigned this Mar 3, 2022
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We need to update also the M2J matrix @gsisinna as one is the inverse of the other.

I would do further checks then.

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Good 👍🏻

@pattacini pattacini merged commit e0cdbb3 into robotology:master Mar 3, 2022
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2 participants